Season Wrap up
Since its been so long since i last updated this, i will do my best to summarize the last bit of our racing season. We drove all the way to Las Vegas to compete in the PRA Bugorama event. After a LONG drive (18 hrs one way) we made it there and on the first pass, or way up to the lanes, we picked up a piece of glass in the front tire. Not able to make the pass because of a horribly flat tire we had to sit out round one. We were able to fix the tire but that first qualifying pass was our only pass due to the crazy Vegas rain. After convincing the track personnel to let us run we got on the ladder (qualified on the very bottom but still a chance). First round did the burnout and started heading to the line. Staged and tried to hit the limiter when....BLAHHHHHH the car wouldn't rev and would not get off the line. We lost first round which was a VERY long way to drive without even getting a few feet down the track. We still had a great time in Vegas so the entire trip wasn't a waste but it would have been a heck of a lot easier to just fly if we were not going to race!
In the end of the season we only won two events. The other events we attended we were out first round, which very unfortunate. We took third place in the NIDRA points series because of the two event wins and the PRA, we were wayyyy in the back of the points chase.
Bremerton NIDRA July 17
Finally broke the losing streak!!! For this race we are not trying too many new things, just working with what we have on a better track than most we race at. This event we qualified 5th out of 10 cars which put us in a tough position to get any easy breaks throughout the day. We ended up winning all four rounds to take the win! Not only that but we also took closest to dial award in eliminations as well as best light. First round win of the year and the first event win! And to top it off there wasn’t any easy rounds (no red lights or byes).
Bremerton NIDRA July 18
Not quite as good as the first Bremerton event but sometimes you got to learn the hard way. First round of eliminations I turned on the big red bulb by -0.020 seconds. As much as I hate to say it, I don’t think I was early but rather that the car reacted differently. What we decided is that we were working on the 60’ of the car and we had it on the edge too much and it was hooking up too hard. The weather conditions changed and with all of the rubber from the V8 cars we missed the setup. Secondly the clutch was gripping WAY too well popping the car out of the lights. In the end a loss is a loss but I think we learned a bit from this one again.
Portland NIDRA August 1st
After doing an inspection of the clutch I decided it was hooking up too hard for where I wanted it set. I resurfaced the disk to see if we could get a different result. First pass the track was in terrible condition and we ended up wasting (so much for seeing if the clutch resurface did any good or not). Making a few minor adjustments and heading back up the car worked a little better even on the sadly prepped track. At the end of the day we ended up winning five rounds (no freebies) to take the event win out of 19 cars. And to top it off I grabbed the closest to dial in eliminations for a few extra points. I believe with this event win I have taken the lead in points (however at this time I cannot confirm as they are not posted).
Due to unfortunate work scheduling conflicts I will not be able to make the upcoming Woodburn event which takes me pretty far out of the points chase. As disappointing as it is, its still about having fun and that’s what we will keep doing!!!
Test and Tune Yakima May 14, 2010
In preparation for the second PRA S/C race in Sacramento in two weeks, we decided some testing with the car was in order. We went to the local track for some practice in the T&T lane. It was an evening testing so it should give us similar conditions for Saturday night qualifying in Sacramento. Trying a more conservative tune than we were used to because we wanted to see how much the car would slow down. First pass car doesn’t launch at all and goes directly toward the wall. Getting out of it netted a pass of 11.6. Next pass the same tune was in the car, and with a better launch the car went 11.1. Cool now we can get the car to slow down even in great air. The last pass an aggressive tune went into the car which would be what we would run in the heat. This pass resulted in an ET of a 10.79. Overall it was a great testing session. We learned a valuable lesson on track temperature, got a rough tune on the car, and some practice at the tree.
Sacramento May 29-30
After our leisurely trip down, we got in about midnight to have a few drinks with the guys and hit the bed. Next morning, after waiting for what seemed forever to get let into the track, we made it in at about 1 PM. We setup the pit area for the weekend and prepared to make a test pass. Test pass was dead on the index running a 10.906. Now for the first qualifying pass, same exact pass as the test except a tad too fast at a 10.880 must have misjudged the cooling air. For the second qualifying pass I decided to play it a little too safe and ran an 11.06. Oh well at least it’s not a pass too fast for the index and we can relax and enjoy the evening.
In the morning, running the car the same way as the passes the night before the car went 10.98 which would better our final qualifying position to 5th. This made our first round match up with Dave Bendig. First round came up, I cut a good light a .051 to Dave’s .061. When it came to the top of the track I just didn’t take enough thinking I was already on a good pass and the win light came on for Dave. We ended up running right at 11.0 which was pretty dang close to the index but not close enough. Very disappointing first round loss for us but hey I guess that’s just racing.
On out trip home we got about four hours out of Sacramento and we started having motor home problems. After calling mechanic after mechanic we couldn’t get anyone to look at it. We limped the vehicle almost home when it pretty much quit all together. We called a mechanic who could come look at it but not until the morning, so we spend the night alongside the road. Turns out we got some bad diesel somewhere and the fuel filters were plugged after 4000 miles. A quick filter change and we were on the road again.
What a long weekend, leave on Friday morning get back on Tuesday afternoon. And to make it worse racing did not go that well. I guess we will just have to make it up in Woodburn next weekend.
Between Races June 3rd
Woodburn NIDRA June 5th
So far it’s been a rough start to the season. The car will get checked out during this off time and hopefully find the reason for the mystery “bog” from last race. The decklid seemed to work great, however a little difficult to get used to. Hopefully after some finessing with the fit of the fasteners it will be more manageable.
The whole Phoenix crew
Next up… hopefully a test and tune before Sacramento!!
Thursday night before
the test and tune we installed a new shifter box bushing thinking that that was
the shifting issues that we were having last year. The bushing turned out great but the gearbox
must have gotten messed up with all of the beatings it took with the failing
part last season. Friday morning dad
heads off to Bremerton for a thrash gearbox fix. Thanks to Dennis we were able to get the box
fixed and ready for some more abuse. So I
drive home from Pullman for a late night gearbox install and tying up any lose
ends on the car. Everything went as
planned and we were off to Woodburn in the morning (well after a few hours of
sleep anyway).
